Author(s): J. P. Britton; S. K. Askelson; C. M. Budai; D. H. Scofield
Linked Author(s):
Keywords: Tunnel; Heave; Steel ribs; Shotcrete; Mount St. Helens; Spirit Lake
Abstract: The 18 May 1980 eruption of Mount St. Helens resulted in one of the largest debris avalanches recorded in history. The debris avalanche blocked the natural outlet of Spirit Lake. To prevent an uncontrolled and catastrophic lake break-out, the U.S. Army Corps of Engineers (USACE) constructed the Spirit Lake Outlet Tunnel from 1984 to 1985. Because Spirit Lake is located in the Mount St. Helens National Volcanic Monument, the project was transferred to the U.S. Forest Service (USFS) for ownership and management. During original tunnel construction, the most difficulty occurred within the 90-m-wide Julie and Kathy L. shear zone complex. In 1996, tunnel walls within this complex experienced significant convergence, which required major repair along a 30 m segment. During inspections in 2014 and 2015, a 10 m segment at the upstream end of the complex, which had experienced slow heave in the past, was observed to have experienced an increase in heave of approximately 0.6 m, which decreased the hydraulic capacity of the tunnel below acceptable limits. The USACE, in accordance with and with funding from the USFS, designed a repair based on the rib set-shotcrete support system that was used for the 1996 repair. In addition to removing and arresting the heave, the 2015 repair was sized to be compatible with a future potential rehabilitation involving stabilizing and re-grading the invert profile of the Julie and Kathy L. shear zone complex. The 2015 repair construction contract was awarded in September 2015 for $3 million.
DOI: https://doi.org/10.15142/T3170628160853
Year: 2016